Starting with serial number 3000, a major update to the K2 transceiver took place. The main modifications required to bring an older K2 up to date are described in Elecraft’s memo and in the older short list.
The following table shows the same modifications in an alternative view, adds some minor modifications taken from a comparison between the schematics, and offers some of the background for the modifications as well.
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Reference |
Description |
Comment |
Complexity |
Source |
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|---|---|---|---|---|---|
Basic K2: Improved Performance |
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× Better grounding of crystals X7-X11
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Improved IF stop-band attenuation |
Important, real perceivable improvement of receiver’s stopband attenuation |
Tricky soldering of ground wires to case of crystals. Risk of ruining a crystal. |
8. |
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× Rewiring from balanced to unbalanced audio pot
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Removes scratch noise. |
Important for removing the nuisance of a scratchy AF pot, also gives an AF control with smoother characteristics, and makes it possible to turn AF completely off. |
Requires modifications to all three circuit boards. |
9.
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More sinusoidal waveform for easier zero-beating |
Filters out harmonics of otherwise square wave sidetone. See also TF3MA’s improved filter |
1 resistor, and an inductance (47k + 82mH) |
10.
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WJ4P |
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Some RF gets into current sense circuit on 160/80 m |
Simple to do (control board) |
Make C42 0.1 µF (100 nF) |
10.
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(There was a C44 parallel to R7 up to serial #3077, but it should be removed) |
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Replace L33 with one wound on T44-7 core // 5.1M resistor |
Reduces BFO temperature drift to about 25%. |
New L33 can be purchased from Elecraft |
5.
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Remove X2, parallel RP2 with R19=2.7k, check that pulling range is >10 kHz and recalibrate |
Reduces PLL/VFO temperature drift to less than half. |
Note that a too low value for R19 was recommended for a while |
5.
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KD5NDB/Elecraft? | |
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AGC activates on noise only |
Need for this mod is greatest for K2’s with an 8V supply on the high side |
Decrease R1 on control board or use a pot to adjust U2 pin 5 to 3.90 V. |
10.
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'Flatter' SSB filter response |
Important, gives real improvement of SSB receive quality
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Remove one C, add 2 Cs, 2 Rs, and a transistor |
7.
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Weird behavior around 7185 kHz. |
Important and easy to do |
Add two components (Replaced RFC11 may be reused) |
2.
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Basic K2: Intermodulation, image rejection, spurious output |
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Less radiated RF from post-mixer amplifier into IF signal path |
The first measure to try against intermodulation from strong stations |
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3.
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Narrower bandpass filter, better stopband attenuation |
Reduces intermodulation from 18m broadcast band, also increases image rejection in 15m band (from 25m broadcast band) |
Change C30, C33, C36 |
4.
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Narrower bandpass filter, better stopband attenuation |
Decreases spurious output, and increases image rejection in 12m band. Makes the 10m band 1.2 MHz wide (e.g. satellite operation will suffer some sensitivity, See alternative 10m filter options) |
Change C42, C45, C48 |
6.
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Improved Automatic Level Control in VFO for reduced spurious output |
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Change/add a few components |
6. |
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Basic K2: Miscellaneous |
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× DC blocking capacitor for the aux RF connector
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Prevents damage to the output stage if the battery or aux power connector is plugged into the RF connector by mistake |
Cut PCB trace and put a 0.047 µF (47 nF)/50V cap in series with aux RF connector. |
3.
(Capacitor included with KPA100) |
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Improves tx efficiency and allows use of lower supply voltage for charging battery |
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Replace D10 |
3.
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×Series resistor for ESD protection of microcontroller VRFDET input. |
820 ohms series resistor from pin 10, P4 to pin 2, U6. |
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Cut one trace on PCB |
10.
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×Improved Aux bus filtering for increased noise immunity |
Improved filtering out of MCU and into RF board IOC |
Prevents aux bus problems with KDSP2 + KAT100 for e.g. KNB2 |
Change R6 to 100 ohms, C12 to 0.0027 uF (ctrl), R64 to 100 ohm (rf) |
3. & 10.
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Improved keyer noise immunity. Improved auto-detect for straight key. |
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×Changed some time before #3000 |
Change R1, R2 on RF board to 220 ohms |
3.
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12 pF in parallel with 20/30 m band-pass filter trimmers |
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Add two capacitors |
4.
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>Sidetone source is permanently at U8-4 + added RS232 TxD line |
Sidetone source had previously to be changed from control board U6-25 to U8-4 for the KIO2/KPA100 |
U8-4 is now sidetone source and U6-25 is TxD line as required by the KIO2 and the KPA100 |
Connect U8-4 to gate of Q5 + connect U6-25 to P4-1 (Aux I/O) and bypass w/ 0.001 uF. |
10.
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Change 40m bandpass filter to combined 40/60m operation + add varactors to VFO |
Adapt LP filter and tuning range of VFO to combined 40 and 60 m operation |
Ready for 60m option K60XV. |
Change C225, 226, 227 and L25 and L26. Replace C70 with D19, D20 and R29 on RF board |
(Not in list) |
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×Replace voltage selector switch on control board with jumper block |
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It was too easy to move the switch by accident, and then lose the power supply voltage reading |
Simple to do.
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(Not in list) |
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R60 100 ohm pot replaced with 100 ohm resistor |
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There was no need to adjust bias of PA stage, so the pot is not required. |
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(Not in list) |
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Items marked with × are implemented in my K2, while ¤ denotes modifications that I have tried, and then removed.
First version 8 Nov 2002, last update 15 Oct 2006.